Gujarat Narmada
Valley Fertilizers Company Limited.
This paper aims at sharing experience gained from Energy Conservation
efforts at GNFC. The paper is divided into mainly following topics.
1.Introduction
- Understanding the Energy Conservation
- GNFC’S Efforts for Energy Conservation.
- Continuing Quest for Reducing Energy Consumption at GNFC.
- Steam Trap Management
4. Road Map for Energy Conservation.
5.Conclusion
Submitted to :-Bureau of Energy Efficiency
Ministry of Power, Government of India
By :
M.N.Tekchandani-Sr. Mgr(Energy Cell), D.D.Patel-Sr. Mgr (Tech.Services),
N.P.Karvekar-Sr. Mgr(Tech.Services),
D.D.Vaishanav-Manager(Energy Cell),
Gujarat Narmada Velley Fertilizers Company limited, Naramadanagar,
Bharuch ( Gujarat) - 392015
Energy Management and Conservation at GNFC
M.N.Tekchandani-Sr. Mgr(Energy Cell), D.D.Patel-Sr.Mgr (Tech.Services),
N.P.Karvekar-Sr. Mgr(Tech.Services), D.D.Vaishanav-Manager(EnergyCell),
Gujarat Narmada Velley Fertilizers Company limited,
Naramadanagar, Bharuch ( Gujarat) - 392015
Preamble :
Today we realize that our Industry is passing through a very turbulent
phase, where “ Survival ” has become the watchword. This is so mainly
because of
? Removal of Subsidies and Protections
? Globalization, Liberalization and opening up of Industrial sector
to International Competitiveness. Indian Industry finds itself exposed
to external pressures in form of Price, Quality, Environment, Customer
Orientation, Requirement of Services and therefore is busy in making
introspection of its operations, costing, competitiveness and consequent
consolidation. Energy being chief contributor to these factors,
the pressure on reducing and rationalizing energy consumption can
well be understood. In the foregoing paragraphs attempt is made
to look at various aspects involved in handling Energy in Industrial
operations.
Roots of Energy Conservation Conservation: -
The fact remains that Movement of Energy conservation in Industry
is quite old with its visible roots lying in the Oil Crisis of 1973.
Developed Nations took immediate steps to neutralize sudden jump
in oil prices. They pulled themselves out of the storm by institutionalizing
the Energy Management structure, Energy Audits, Practices of Energy
Conservation in a very systematic way and brought all these in to
focus of top management. The drive was already there in form of
rising input costs. These practices resulted in to saving of millions
of oil equivalent in case of number of Industries like Union Carbide
USA, Dupont USA ,Courtaulds UK.
[A]UNDERSTANDING ENERGY CONSERVATION:
“We cannot Manage What we do not understand ” goes saying from
an expert. It assumes specific significance here when we address
the issue of Energy Management. Therefore it will be worthwhile
to first understand as to what is Energy Conservation and when we
address this, we realize that Energy Conservation (En Con) is the
subject of Contemplating, Soul Searching and Self Questioning on
? What is the Energy Consumption of My Unit?? How and where Energy
is used?? How much is really required?? What can be done to reduce
energy consumption
ENERGY CONSERVATION AND THERMODYNAMICS:-
The second law of Thermodynamics determines that Quantity of Useful
Work we obtain is
smaller than the potential of original Energy form. Therefore
Ideally Energy Conservation
means reducing the proportations actually wasted to lowest possible
level.
B]GNFC’S MARCH TOWARDS ENERGY CONSERVATION:
In the foregoing paragraphs attempt is made to give an account
of strides taken by us for Energy Saving. Following picture gives
an idea of methodology employed.
In foregoing
paragraphs, few examples of above measures are discussed.
1). Operational changes: At GNFC , we follow the LOOK, LISTEN
and FEEL concept to improve / overcome problems and for maintaining
uninterrupted operations . Developing Understanding of the process
by simply monitoring operations, we can save energy . Some of the
examples are as given below :-Examples:¾ Separation of plant air
header (80KW): We modified the system so that plant air compressor
(Pres. 4.0 barg) system is separated from instrument air compressor
(7.0 barg) which lead to the power saving of 80 KW.
¾ Elimination of 2nd stage of fluidized bed cooler
(FBC) in ANP plant (55KW)
From the operating experience it was observed that most of the
cooling phenomenon was getting completed in 1st compartment of fludized
bed cooler making 2nd compartment redundant. Therefore with the
help of ducting modification , 2nd chamber was by passed. This led
to stoppage of blower supplying cooling air to 2nd stage and resulted
into power saving of 50KW.
¾ Cooling Water recovery in Ammonia Plant:
Earlier our cycle of concentration (COC) remained around 3. Practically
blow down from sump basin was almost nil and major blow down was
done locally in the plant. To increase the COC, local draining of
cooling water from number of users in section 200/300 of Ammonia
Plant was arrested by conducting a survey and diverting this open
drains back to basin through specially laid piping. This has helped
to increase COC more than 5 and accordingly cooling water treatment
is modified to take care of fouling in the exchanger.
¾ Flow orifice checking for higher-pressure drop.
Originally we had only Ammonia & Urea complex. Subsequently
we have added Nitro complex, Methanol –I & II, Acetic Acid,
Captive power plants. Due to this our utility consumption has increased.
This has led to increased pressure drop across orifice for Inst
air , DM water and other utilities piping. We have replaced orifices
which were offering high-pressure drop.
¾Identification of Additional pressure drops in the system.
We have removed check valve and unwanted flow measurement system
offering higher-pressure drop installed in raw water supply pipe
at Utilities Plant
2). Reliability building :
9 Identify equipment / system limitation for uninterrupted operation.
9 Sustained operation reduces start-up, shutdown losses.
9 Sustained operation increases production, which reduces energy
consumption
¾CO shift section revamp in Ammonia plant (making shift reactors
parallel) : Due to changes in feed oil quality, increased soot and
nickel on catalyst bed of CO shift reactor was leading to Ammonia
Plant stoppage once in 4 months. After working of suitable action
plan, two of the three shift reactors were made parallel through
piping modification. this has prolonged our continuos operation
span to nearly one year.
¾Quench ring modification : Frequent quench ring failures were
resulting into gasifier shut down in Ammonia Plant. With operating
experience and nos. of trials we could successfully modify the design
of quench ring. Consequently we are able to operate the gasifiers
much longer.
¾Additional feed oil pump in Ammonia plant : Due to the requirement
of frequent maintenance of feed oil pumps for gasifiers in Ammonia
Plant, additional pump has been installed and we are achieving higher
on stream days now.
¾Refrigeration compressor modification to reduce speed below MCS
: From the operating experience it was observed that for refrigeration
compressor of Ammonia plant, max. load was on HP Barrel. In view
of this HP barrel revamp was carried out in April 2000 with higher
improved internals. With this change, operating speed has come down
on one hand where as chiller pressure and synthesis loop pressures
also remain lower.
3).Recycle & integration of operations :
The streams which were sent for processing in original design,
were analyzed and reviewed. With operating experience , it was realized
that some of the streams did not require processing , so they were
recycled directly. Some examples are as below :
¾Turbine condensate recycle to deaerator : The huge quantity of
condensate which was design to be processed in DM plant was recycled
to the deaerator in Ammonia plant. This saved on processing &
pumping cost.
¾DM water re-circulation during gasifier start-up & cooling
down : The DM water which was used for startup & cooling down
after shut down in gasifier was recirculated by installing the required
system minimizing on DM water consumption.
¾Condensate recovery in Thermax Boiler. In our boiler SCAPH outlet
heating coil condensate from steam traps was discharged in open
channel. It has been diverted to deaerator by replacement of trap
with suitable orifice. The recovery of condensate is made along
with its heating value.
¾Waste water of Urea plant in Ammonia plant as make up. Wastewater
containing about 50~100 PPM urea and 50 PPM Ammonia, was earlier
discharged to ETP for treatment. On other end in our Ammonia plant
we needed DM / steam condensate for reaction in CO shift section.
This make up of water is carried out in carbon extraction section.
We are using urea plant wastewater for this make up purpose. In
Gasifier at higher pressure and temperature Urea decomposition takes
place. We are also using same wastewater as seal flushing water.
4). Use of latest technology :
The technological advancement is a continuous process through
operating experience and new research. We monitor such developments
and adopt them whenever and wherever feasible. Some examples are
as below :
?S-200 basket for synthesis reactor by M/S Topsoe (Saving of 1580
kwH power) : By going in for Energy efficient reactor basket design
of S-200 configuration from M/S Haldor Topsoe . We could reduce
the synthesis loop pressure as well as circulation rate and resulted
into energy saving of 1580 KW.
?Installation of vertical decanter : We are facing problem with
horizontal decanter in soot recovery section in Ammonia plant. Same
was replaced with better performing newly developed vertical decanter
which gives superior soot separation.
?Conversion of control system from pneumatic to DCS system :The
Ammonia plant Instrumentation and control system was converted from
pneumatic to DCS system / PLC control system. This has resulted
into smooth operation as well as helps us in quick diagnosis of
a plant problem. This conversion was carried out without any special
shut down for the same, most of it being done on line.
?Installation of Ammonia Absorption type refrigeration. : Conventional
Air conditioner unit is consuming more electrical energy. After
more than 20 years of operation they were more prone to maintenance
and refrigeration media used was Freon gas, which is harmful to
atmosphere. We have replaced it with Ammonia absorption type refrigeration
system in our Ammonia plant. The refrigeration load is 110 TR. This
is based on steam and consumes less energy
?Retrofitting tower : Tray modification in distillation towers
of Methanol –I/II plants have resulted in to reduction in the steam
consumption.
?Replacement of MeOH- I Plant synthesis reactor with latest energy
efficient iso thermal Reactor has resulted into saving of steam
to the tune of 150 T/day. Similar replacement with iso thermal reactor
is being planed for the MeOH-II plant.
Page 6 of 18 ?Replacement of MeOH-I plant distillation column
tray with high efficiency trays has reduced the energy consumption
significantly as well as resulted into capacity enhancement.
?Replacement of column packing with latest development packings
in Formic Acid plant . We replaced the standard RAUL ring packing
with latest design SLVK packing which has better HETP for almost
same packing factor. This reduce the steam energy required per MT
of Formic acid processed in the column.
5). In house innovations & debottleneck :
For debottlenecking of single equipment/ part system, external
consultant becomes very costly. After 20 years of operational experience
and operating data , gradually we have developed better understanding
of process. We can carry out in house process engg to debottleneck
equipment/system. For physical property prediction at different
operating conditions , process simulation / design softwares can
be used . This becomes clear from our following schemes.
? Stripping of H2S and recovery of Ammonia from process condensate
generated in CO shift section of Ammonia plant:
This innovative process was used for stripping of H2S and recovery
of Ammonia from process condensate. The waste tail gas stream from
rectisol wash unit of Ammonia plant contains about 80% CO2 and 20%
vol N2, is used for stripping H2S from 150 PPM to less than 0.5
PPM in condensate stream of 6 m3/hr retaining Ammonia in process
condensate. The condensate containing 1% by wt. Ammonia is processed
in wastewater section of urea plant and thereby reducing treatment
cost and pollution in atmosphere.
?Debttlenecking of Ammonia absorber tower in urea plant. After
detail study and with the help of computer process software, the
tower is debottolnecked from tray tower to packed tower. Consequently
Ammonia venting to atmosphere is arrested resulting in to saving
in Ammonia.
?Methanol water distillation column revamp which included rerouting
of reflux steam and shifting of critical tray location for temp.
Control. Consequently Tower performance has improved significantly
and Methanol slippage has reduced by 40 MT/year This was arrived
at by rigorous analysis and process simulation.
Capabilities built up at GNFC:
In order to support innovations & debottlenecking, we have
developed in house process engg capabilities as per following.
| ? |
Aspen process simulation software |
| ? |
Chemcad simulation software |
| ? |
HTFS heat exchanger rating/design |
| ? |
Chempro xlt :This software help in evaluation of heat exchanger,
control valve, |
|
orifice etc. |
6). Optimization and rationalization:
During design stage , design is carried out with certain assumptions.
In actual operation , based on actual data there is always scope
for optimization . The examples are as under : a).Pumps
Pump Impeller trimming:
Normally system designer keeps margin for smooth operation of
pump. We could identify pumps, which were operated with discharge
valve throttled due to developing of higher head than required.
We collected operating flow versus. head data and compared it with
performance curve given by supplier. Based on head requirement we
decided to trim the impeller and saving has been achieved in electrical
power. The table highlights some examples and benefit gained.
| Pump number |
Service |
Saving achieved |
| P-1846A |
Condensate transfer pump in Ammonia plant |
65 KW |
| P-1711 A/B |
Service water pump in raw water plant |
14 KW |
| P-1845D |
DM Water transfer pump |
18KW |
| Guard Pond Eff.Water Pump |
Water make up for Ash slurry preparation |
Intermediate operation saving 4 KW |
| C.W make-up pump |
CW make-up pump impeller trimming |
68 KW |
Replacement of pump with lower head In case of following pumps,
head requirement was found to be less than specified , which could
not be met by impeller trimming. In such cases new lower head pumps
have been installed.
| ASDS Pump |
Bottom ash slurry disposal |
8 KW |
|
pump in Boiler |
|
| P-1705 |
Water supply from factory to |
18 KW |
|
Township |
|
Separate pump with lower head
In Ammonia plant cooling water pumping system was designed for
50 meters. head. However our close review revealed that there was
only one heat exchanger which necessitated such higher head. Therefore
segregation of the same by installation of a small capacity booster
pump, we could reduce significant power consumption for main cooling
water pumps.
b).Study of FD fans for Boilers and replacement with suitable
size
Originally FD fans were designed to meet higher head requirement
of furnace draft and Steam Coil Air Preheater (SCAPH) . Subsequently
we had a problem of SCAPH choking due to coal ash. Hence it was
removed. This resulted into lower system resistance and FD fans
suction guide vane remained in throttled condition. After making
assessment of system requirements, three new FD fans having lower
head have been already installed and remaining three are to be installed
in April’04 shut down. The power saving realized is 55 KW per fan
and total power saving is likely to be about 330 KW.
C). Identification of new low capacity Combustion air blower C-1301
for Steam super heater in Ammonia plant.
Based on our operating experience, the blower was found to be
too much over sized in the present operating requirements, as the
load on super heater has also reduced over a period on account of
diverting tail gas for other productive uses. Field performance
testing was carried out and system curve got established. New specification
has been prepared for a new smaller size blower. This has a potential
of saving upto 40 KW.
d). Reduction of boiler blow down
Passing of blow down valves was resulting into silica level of
0.1 ppm against normal value of 1 and max. allowable 1.8 PPM. This
was resulting in to high-pressure energy let down to lower level
and some steam venting at atmosphere steam level. We have replaced
blow down valve to arrest passing of valve and pH is maintained.
Silica levels brought back to around 0.8 to 1 ppm i.e. near to normal
value. This has reduced venting of 3 to 4 MT atmospheric steam.
e). Installation of additional low head condenser transfer pump
in Urea.
Originally high head pump was installed to cater demand of process
flushing in urea plant and the balance( about 75% ) quantity is
being transferred to Utility plant for polishing which actually
needed lower head. We have developed a scheme to segregate lower
and higher head requirements and separate pumps are envisaged as
per head requirement for process flushing and remaining to be sent
to utility plant. New low head pump specification with control logic
is prepared. Pump is being procured.
7). Keeping a close watch on key equipments:
z Monitoring of Compressors
Every month we are collecting operating data of compressors/ Turbines.
Stage wise efficiency and turbine efficiency is calculated by using
process simulation software ASPEN. This helps in keeping a check
on performance and preventive maintenance of compressor.
z Monitoring of Exchangers
Every month we are collecting operating data of Exchangers and
use of process simulation software is carried out for performance
checking of exchangers. This helps in monitoring of performance
and planning for cleaning during shut down.
zMonitoring of CT tower and performance evaluation. Regularly
we are collecting operating parameters of all plant cooling towers
and compare the CT approach temperature with design by using performance
evaluation chart.
zInstrument Air consumption shooting up at times: Site survey
conducted to reduce consumption. Installation of flow devices at
various locations have been envisaged after detailed network study
to carry out balance and monitoring.
zVacuum hold up test for identification of leakages in condenser
and improve vacuum. During shut down, vacuum hold up test is carried
out to know leakages in vacuum system. The allowable vacuum drop
rate is 3 MM Hg. If it is higher then the leakage is identified
by filled up water in shell side of surface condensers.
Some of Electrical Measures recently adopted at GNFC
? Six numbers of Lighting Transformers Ordered for reducing lighting
voltage ? At few locations Lighting Voltage reduced by changing
tapping of Transformers ? Change of Lighting fixtures in office
are of Corporate building ? Delamping of plant area after closely
reviewing judicious requirements. ? Experimental use of Transparent
roofing sheets at an interval of about 15 meters for making use
of
natural light have lead to reduced requirement of lighting in
day time in two of the coal conveyor gantries.
[C]CONTINUING QUEST FOR REDUCING ENERGY CONSUMPTION
A separate Energy Cell has been formed within the the Technical
Services for exclusively focusing on Energy Issues in close coordination
with other ongoing efforts. The initiatives taken by Energy Cell
are
(a). Evolution of Steam Trap Management at GNFC
Following action were taken
- Compiling trap identification list for each list for each plant
jointly with operating group.
- Evolving Tagging system for traps.
- Trap identification, listing carried out plant wise.
- Traps have been tagged in field as per the identification list
details.
- A Demonstrative Steam trap Audit for selected 200 nos. of traps
carried out in Hazardous Chemical plant with the help of Experts
M/s Forbes Marshall team. During this some of the engineers were
trained for use of Ultrasonic leak detection technique and other
observations.
- A one-day training programme conducted for Engineers and technicians,
giving information on Trap Basics, Application, Use and Maintenance
techniques.
- In house steam trap Audits carried out in most of the plant-using
instrument Ue-2000. The trap functioning status was observed to
be as per following.
| Total Traps |
: |
2082 |
| Traps Audited so far |
: |
1751 |
| Defective traps identified |
: |
622 |
| Defective % of Total Audited traps |
: |
35 % |
Apart from this, some of the traps found to be of wrong type,
improperly installed. For some of the traps, expert opinion was
also sought. A guesstimate of steam loss through these traps was
made using information available from trap manufactures. Total quantity
of steam which can be saved works out to be 5.4 MT/hr. The corrective
measures for the same are as under way.
(b). Energy Audit of Fans / Blowers :
From our observation of the throttled dampers / guide vanes, we
selected 17 nos.of Fans having power requirement more than 100 kw
located in various plants for their details Energy Audit. Performance
testing was carried with the help of outside experts per BS 848.
The performance testing revealed that 4 numbers of Fans in Boilers
area are operating at significantly lower efficiency. ( This is
over and above FD fans mentioned in this document in point no 6
- (b)) The scope for saving in terms of power is 256 kW. One of
the main reason for lower efficiency of fan is observed to be operation
at point far away from design parameters. Various technological
options like Variable speed fluid coupling and Variable speed drive
motor system have been worked out to save Energy for which proposal
will be put up to Management shortly.
(c). Detailed study of Equipment (pumps) consuming high power.
For identifying energy saving potential it was decided to take
up study of pumps consuming very high power. Therefore Ammonia plant
cooling water system, which consumes between 5 to 6 MW was selected
for detailed study. From the preliminary data available, it was
observed that these pumps operate at lower efficiencies. Similar
exercise was carried out for Cooling Water pumps of Urea plant and
Captive Power plant In Captive Power plant, one of the pumps was
identified for operating at substantially lower efficiency i.e.
75 %. To improve the efficiency of deficient pumps, new specifications
were prepared for Ammonia, Urea, Captive Power Plant Pumps considering
the changed operating parameters and the same are under implementation.
(d). Insulation.
Insulation is another area, which needed focus from Energy saving
point of view.
1) To begin with, In house survey of Boiler no.II and Boiler no.III
was carried out and at significant number of locations, Insulation
quality found deteriorated which was evident from surface temp.
as high as 90 °C. This was mainly due to lack of reinsulation after
shut down. Out of the identified defects, some have been attended.
2) In Weak Nitric Acid plant temperature of HPSH steam was observed
to be remaining lower than envisaged in design by 10 °C. To evolve
the solution, Insulation audit of affected piping was carried out
and losses were found to be unacceptably high. Various options were
reviewed including replacement with best alternative material i.e.
calcium silicate . Accordingly the cost benefit analysis was carried
out which indicated the steam saving potential of 500 kg/hr. The
proposal is under scrutiny.
? It is also observed that glass wool type of Insulation tend
to sag over a period of time making bottom portion bare which increases
losses. Further more steam consumption increases during monsoon.
It is also being closely reviewed to replace phase wise glass wool
type Insulation with block type Insulation (e.g. Calcium Silicate
type) that has better properties.
3) During the last shut down, Cold Insulation replacement carried
out for 11 nos. Of equipment's operating under sub zero conditions
and for 11 nos. Of piping sections. This has resulted in to reduced
load on Refrigeration section.
(e). Cooling Tower Audit in Captive Power Plant(CPP):
For reducing steam consumption in CPP, Evaluation of Cooling Tower
Parameters was carried out by Energy Cell and it was observed that
CPP cooling Tower performance remains poor in terms of achieving
supply temperature for the prevailing Dry Bulb / Wet Bulb temperature
as well in comparison to other cooling towers in GNFC. Particularly
in summer cooling water temperatures were becoming a limiting factor
for performance of condensers of both TGs and were resulting in
to increased steam consumption. Accordingly in house survey and
assessment of cooling tower was carried out recently, where in physical
inspection of cooling tower components , taking photographs of areas
where significant amount of air short circuiting takes place, individual
cell water temperatures, measurement of water level on deck for
each cell was carried out. Our observations were as per following.
1) Cooling water supply temperature for Cell-3 and Cell-4 was
found to be remaining lower by 3 °C by compare to Cell No. 1 &
2. This indicates that performance of Cell No 3 &4 is poor compared
to Cell No 1 & 2.
2) Major damages of wooden sheets in the fan plenum area leading
to sizable quantity of air short circuiting in all the cells were
observed. The details of the same are as per photographs given below.
3) Openings on the East side A.C Sheeting wall of the cooling
tower - near inspection door , at top near hoist structure joint
lead to lot of false air entry into the cooling tower.
4) Inside the tower , the door between cell no 1 &2, 3 &
4 remains open leads to uneven loading.
5) No.
Of Flower Nozzles (water distribution) on the top deck of cooling
tower are found without orifice cap, which leads to the overloading
of these nozzles and uneven distribution within the cell and poor
mass and heat transfer .The inlet diameter of specified nozzle with
orifice cap is 24 mm and without orifice cap is 32 mm .
6) Average water level height was observed to be 3 cms higher
on southern side deck area compared to northern area indicating
uneven water distribution on cooling tower top deck .
7) In the plenum chamber significant water dripping was observed
in the fan suction area, indicating deteriorated performance of
drift eliminators.
Accordingly an action plan has been evolved to eliminate above
deficiencies.
Following Photograph shows significant damages in Following Photograph
shows significant damages in the plenum area leading to short circuiting
of air plenum area leading to short circuiting of without without
contacting water(Top deck) contacting water(Top deck)the fan at
top deck.
Following Photograph shows significant damages Following Photograph
shows significant damages in near entrance door of wet section leading
to the plenum leading to short circuiting of air without short circuiting
of air without contacting water. contacting water (top deck)
Following
Photograph shows significant damages Following Photograph shows
significant damages in the plenum leading to short circuiting of
air without in the plenum leading to short circuiting of air contacting
water (detection of air leakage). without contacting water (detection
of air leakage).
|